... famous last words indeed. Haven't been able to do any further testing past couple of weeks as I use the car for work and been on some silly shifts. Anyway - was about to get the spanners out and whip the turbo off, but decided to do one last test on the actuator... rather than just unplugging it, I tied the wastegate arm to the aircon bracket with speaker wire. Off I went, not expecting much - came off tescos roundabout, then before I knew it I was boucing off the limiter and for a brief second approached a number I don't even want to think about on the boost gauge...
So... theres naff all wrong with the car other than the exhaust gas pushing the wastegate and actuator open. I'm pretty gutted tbh - the spring in the actuator is only rated to 0.7 bar, and thats what it hits with the boost controller turned off. However, the HKS on my old car ran 0.7 bar exactly the same, yet managed to hold back the exhaust gas with the boost controller cranked up to 1.2 bar... so a bit confused on that front. Unfortunately I haven't got the old actuator and bracket to compare lengths but I'm beginning to think I've been sent the wrong actuator altogether as I said, there are already several washers on the bracket, and the arm is screwed all the way in just to hit 0.7 bar.
So what do you guys reckon? Do I need a stiffer spring and/or more washers on the bracket, or should I just get the actuator replaced for one with a shorter arm? I'm gonna get some longer bolts and more washers just to see how much difference it makes - in the meantime, any suggestions are much appreciated thanks for all your help and patience!